| We tied up to the 
                dock in Urbanna Harbor, VA at 2230 last night from Ft Lauderdale. 
                It was quite a trip. As always things happened we didn't expect, 
                but that's why we go on these adventures. 
 After working three days on Davids new purchase of his 1977 Cal 
                47 foot ketch, we thought we were sea ready. We noticed a smell 
                like hot anti-freeze as we motored the hour long ride down the 
                river to the ocean. We noticed the heat gage a bit hot but figured 
                it would calm down, after all the engine hadn't run in three years 
                and we thought after pulling the needed maintenance it just needed 
                to run for awhile.
 
 As soon as we got to sea we raised sail and cut the engine, headed 
                north at 6 knots in a 10 knot breeze, The boat handle very well 
                and we were all very pleased.
 
 As we got into the Gulf Stream our speed picked up to 8 knots. 
                After my watch I hit the sack and when I woke up we were becalmed 
                and some how got east of the Gulf Stream. We started the engine 
                and it instantly over heated. There we sat for the next seven 
                hours waiting for any kind of breeze. We also found we were in 
                some wierd current pushing us out to sea and in behind the Bahamas.
 
 By noon a small breeze blowing from the south started up and we 
                were back heading north. We weren't to far off our rhumline but 
                weren't in the Gulf Steam only doing 4 or 5 knots. We started 
                sailing westerly looking for the Gulf Stream. With no engine this 
                could take awhile. We finally hit the Gulf Stream sometime the 
                next afternoon and the wind also freashened from the south to 
                about 35 knots. We were moving North at 11 to 12 knots. We were 
                way over powered so tried to get the main down and sail on mizzen 
                and head sail only. Main got stuck. No matter what we tried we 
                couldn't get it down. We doused the head sail, sailing on Main 
                and mizzen but was difficult to steer, seas were getting very 
                rough plus it was dark and the spreader lights weren't working. 
                After about two hours working in the dark, we finally figured 
                one of the lazy jacks got caught in the track and was jambing 
                the main. We had to really yard on the lazy jack to get it free, 
                when we did the main came right down and we re-set the headsail 
                and off we went.
  Me with the Cal 47
  The next morning as we were hauling 
                at 11-12 knots, when we found we were out of fresh water. The 
                fresh water tank had some kind of leak and it went into the bilge 
                and got pumped out. We had three one gallon jugs of water that 
                was rationed to four guys that had to last three days until we 
                got to the Chesepeake. 
 The next night we must of been on the edge of the Gulf Stream 
                as we got caught in some very confused seas cause by contrary 
                eddies. Four and five foot seas were just coming and going from 
                no where. It was very rough and confused, took us about an hour 
                to sail through it.
 
 Next day forecast called for heavy thunderstorms and Northeast 
                winds at Cape Hatteras. That's right where we were going to be 
                so the Captain changed course for Morehead City. Captain didn't 
                want to try and get around Hatteras in rough seas with no engine. 
                Took us all day to sail there from the Gulf Steam and as we got 
                close we had to call Seatow to meet us at the entrance and they 
                towed us to the municiple dock at Beaufort NC. We all took showers 
                and went out to dinner, felt really great after almost four days 
                at sea.
 
 The next day it was determined that the problem was a faulty radiator 
                cap. We got a new one, fixed the water tank and started up the 
                intercoastal. Didn't get far when the engine overheated again. 
                Pulled into Jarret's Marina. Two days there while we found that 
                the heat exchanger was shot. Had to find a new one and change 
                it. Off again, the temp held for awhile but over heated again 
                by the time we got to the Pamlico Sound. We sailed through Pamlico 
                Sound and when we got to Bay River to anchor for the night the 
                engine overheated agian as we anchored. We checked the water pump 
                to find the empeller was ground up to little pieces. We were now 
                in the middle of now where, we were all tired so hit the sack, 
                figured we come up with a plan in the morning.
 
 Next morning, first light, we hailed a waterman pulling crab pots. 
                He came over and we told him our problem. He was a goodman and 
                told us to go up river about three miles to the R.E Mayo fish 
                plant and they could probably help us. He said he would tow us 
                later when he got finished pulling his pots. We told him no problem 
                we had our dingy. We launched the dingy from the davits with the 
                8 HP yamaha and took off up river. The Mayo fish plant was pretty 
                run down and very backwoods North Carolina. When we got to the 
                office, there were four ol' boys sitting in their rocking chairs 
                swapping stories. We told them our problem and at frist they said 
                they didn't know what they could do for us. Then one got up and 
                said he thought he had an old empeller in the back room. He came 
                out and said he didn't but got on the phone to Ray's Marine in 
                Bayboro, about 18 miles up the road. Rays Marine said he had one. 
                We asked if there was a taxi service so we could get there and 
                they said no there wasn't. Then one of the other ol' boys suggested 
                we just take the company truck. The others said sure and off we 
                went. We bought two empellers and hurried back to the fish plant. 
                When we got there we thanked them and asked if we could pay them 
                for their kindness and the use of their truck. They said no, they 
                were just glad to be able to help us. I was really touched by 
                those ol' boys, they made me proud to be an American.
 
  We got back to the boat and put 
                in the new empeller. Ran the engine for quite awhile and took 
                off only to discover an exhaust leak. We tied off to the R.E Mayo 
                docks to fix that. As we left the dingy on the davits got caught 
                on a pielling and we tore a hole in the starboard pontoon and 
                ripped it from the davit. Jury rigged the dingy to the davit and 
                carried on. The Captain was really upset he tore up his brand 
                new dingy. 
 The rest of the day was fairly uneventfull. We made our way to 
                Alligator River where we anchored for the night. Got up early 
                the next morning and sailed across Albemarle Sound. Wind was really 
                kicking up and the weather was turning foul. We tied up at a small 
                Marina at Coinjock to have lunch at a resturant we stopped off 
                last year. After lunch we heard the weather report. We were going 
                to try and make it to Norfolk, VA by night fall and sail the rest 
                of the way to Urbanna that night but we were in a tornando warning 
                area with thunderstorms of 70 mph gust and two inch hail. We stayed 
                right there for the rest of the afternoon and night playing blackjack.
 
 Got up at first light, motored across Currituck Sound, up the 
                Chesepeake Albemarle Canal into the Elizebeth River. Motored through 
                the Norfolk Naval Yard, set sail and sailed all the way to the 
                Rappahanock river. When we got to the Rappannock the wind was 
                blowing 25 right down the river. It was freezing cold at 65 degrees. 
                We motored the last 16 miles to Urbanna freezing our balls off 
                and tied up to Davids slip at 2230 last night.
 
 It was a great trip and I'm glad I went even with all problems. 
                They only added to the adventure.
 
 Semper Fi,
 
 Bob
  
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